1940 Norton Fitzwarren rail crash

Coordinates: 51°01′23″N 3°08′56″W / 51.023°N 3.149°W / 51.023; -3.149
Source: Wikipedia, the free encyclopedia.

Norton Fitzwarren rail crash
Details
Date4 November 1940
03:47
Location
Reading to Plymouth Line
OperatorGreat Western Railway
CauseSignal passed at danger
Statistics
Trains1
Passengers~900
Deaths27
Injured74
List of UK rail accidents by year

The Norton Fitzwarren rail crash occurred on 4 November 1940 between

Taunton train fire
of 1978 was also within 2 metres (6 ft 7 in).

Overview

A simplified track and signal diagram of the Norton Fitzwarren crash.
The train went through the catch (trap) points at the end of the Down Relief (Slow) Line.

The house of the driver, Percy Stacey, had been bombed the previous night. He had gone to work as usual.[2] Further bombing on the night of the accident and other disruptions had made the train an hour late by the time it reached Taunton.

The crash occurred at a point on the railway where four tracks were reduced to two. On the four-track section, the up and down fast lines were in the center between the up and down slow lines. Instead of the usual practice of locating all signals on the same side of their respective tracks (GWR practice was to commonly put them to the right of the track, the same side their drivers stood on the locomotive), the Relief Line signals were on the left, and the Main Line signals were on the right.[3]

Stacey's train left

trap points
were in place, the train was derailed rather than running onto the fast line and colliding with the other train. The fireman and 26 passengers were killed.

The guard in the end vehicle of the overtaking train was alarmed by strange noises, which later turned out to be ballast thrown up by the derailing train alongside. He applied his own brakes to check what might be the problem, the train was stopped at Victory Siding, the next signalbox to the west, and he discovered the sides of the last vehicles were scored from flying ballast, and there were broken windows. The derailing "King" locomotive had nosed down off the end of the overrun siding and then swung across the main tracks, what must have been feet behind the overtaking train.

Also, the signalman at Taunton station had initially cleared the starting signal for the usual route at the west end of the platform, to cross over to the Down Main line, which was showing when the train stopped at the platform. While the train was stopped the signalman was offered the faster non-stopping train, so restored the signal, changed the route of the crashed train from the Down Fast to the Down Slow, and cleared the Down Slow signal. The driver was on the opposite side of the locomotive to the signal, and the fireman, who performed a second check at departure, reported as usual "it's clear". Because of the slow speed of departure, in blackout conditions, the driver never noticed they were now continuing on the Down Relief line and not taking the crossover to the Down Main.[3]

The signals had been badly placed as an economy measure. If at least one pair of signals had been placed as usual – requiring a gantry or a bracket – then the driver of the train would have been more likely to recognise which track he was on and which signals related to it.

The extra space between the Fast lines was a holdover from the wide

track centres of Brunel's broad gauge.[4]

The signals at

Automatic Train Control
(ATC) which alerted the driver, in the cab, audibly that the approaching distant signal is at "caution". A warning signal has to be acknowledged or the brakes are applied. Drivers can be so used to cancelling the warning, that they may do this subconsciously. This would especially happen if the driver is reading the wrong green signal. Although the ATC equipment was working correctly, wartime deferred maintenance had meant that in a number of cases the ATC ramps were not working correctly and were giving false "caution" alerts when the signals were clear, supposedly a correct failure mode but one which led to crews believing that a warning when they saw clear signals was just another maintenance issue.

Inquiry

The inquiry was conducted by the Chief Inspecting Officer of the Railway Inspectorate, Sir Alan Mount. He concluded that although the position of the signals was confusing, the "sole cause was an unaccountable lapse on the part of Driver P.W. Stacey" despite his excellent record of 40 years of service. He suggested that operating under conditions of blackout and the general strain of the war, including Stacey's own house being bombed the previous night, may have been a factor in this lapse.

Wartime censorship

This accident was reported soon after in newspapers in far off Australia. The cause was attributed to a culvert washaway caused by recent heavy rains, and no mention was made that the locomotive was a namesake of the reigning monarch.[5]

Aftermath

Despite a considerable amount of sympathy for Driver Stacey, he never forgave himself for the accident. When asked for a comment by the press, he said "don't talk to me, I'm a murderer". He died just over a year later for no apparent medical reason.

See also

  • List of train accidents

References

  1. ^ "The Norton Fitzwarren Train Disaster". Taunton Courier, and Western Advertiser. 9 November 1940. Retrieved 20 October 2015 – via British Newspaper Archive.
  2. ^ "Report on the Norton Fitzwarren Train Disaster". Taunton Courier, and Western Advertiser. 4 January 1941. Retrieved 20 October 2015 – via British Newspaper Archive.
  3. ^ a b "Accident report by A.H.L. Mount" (PDF). Railways Archive. Retrieved 20 October 2015.
  4. .
  5. Weekly Times
    . No. 3725. Victoria, Australia. 9 November 1940. p. 3. Retrieved 24 July 2017 – via National Library of Australia.

External links

51°01′23″N 3°08′56″W / 51.023°N 3.149°W / 51.023; -3.149